1 (edited by eric.s.hall.em 2017-05-11 16:10:21)

Topic: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

I just purchased the Filastruder 2.1a kit and assembled it.  One pound of ABS was extruded successfully.  I purged the ABS and then added the Eastar 6763 PETG pellets and extruded about 20 meters at 190 C this weekend.  Then tonight I attempted to extrude more PETG but the filastruder was seriously damaged.  I waited for 20 minutes after the temperature reached 190 C and about 2 meters of PETG extruded.  The temperature went down to 165 C and the auger pipe started twisting and I could hear the gearbox sputtering.  I took it apart and took pictures.   

I did adjust the CV and CC knobs on the stall protection board.  What do I do now?

Post's attachments

broken_extruder1.jpg 51.25 kb, file has never been downloaded. 

broken_extruder2.jpg
broken_extruder2.jpg 59.35 kb, file has never been downloaded. 

broken_extruder3.jpg
broken_extruder3.jpg 55.09 kb, file has never been downloaded. 

You don't have the permssions to download the attachments of this post.

2

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Has anyone tried a 1/2 inch hole for the pellet port into the auger pipe?  As you can see in the attached image, the 1/2 inch hole is much smaller than the one that comes with the kit.  Is it necessary to have a long hole?

http://soliforum.com/i/?ddKyOre.jpg

3

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

eric.s.hall.em wrote:

Has anyone tried a 1/2 inch hole for the pellet port into the auger pipe?  As you can see in the attached image, the 1/2 inch hole is much smaller than the one that comes with the kit.  Is it necessary to have a long hole?

I have not tried using a smaller hole, but you may have two issues doing it that way.

First, Does the pipe you are planning to use have a weld strip down the length of the pipe?  If so, the auger will likely start to rub on it and put metal particles in your filament.

Second, The smaller opening might have an issue with feeding the pellets into the pipe.  I know from my experience that sometimes the pellets don't feed well with the large opening.

It would be a good idea to figure out why the pipe bent in the first place otherwise you will likely have it bend again or damage the motor even more.

-os3dp

4

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

os3dp wrote:

It would be a good idea to figure out why the pipe bent in the first place otherwise you will likely have it bend again or damage the motor even more.

Working this troubleshooting out with the customer via email as they emailed as well. I agree that the smaller hold will probably cause some inconsistent feeding issues.

5 (edited by eric.s.hall.em 2017-04-11 19:20:38)

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Yes the pipe I bought at Lowes store has a weld line, thanks for mentioning that. 
I am working with support to figure out why the pipe bent now.  Tim asked to hook the heater to the output of the stall protection board and get the amp reading.  The stall protection board indicated 2.84 A at first but then went down to 1 A and then 10 seconds later jumped to 2.84 amps for a 1/2 second a few times and then went back to 1 A consistently.   The led red and blue lights are on all the time and the heater heats up.   I had originally followed the V2.1a PDF file instructions to turn the CV and CC knobs left till the soft click and then turn the CV 15 turns and the CC 7 turns clockwise.

6

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Here is a history leading up to the failure:

1) I successfully extruded the 1 pound bag of ABS pellets that came with the Filastruder
    a.  While extruding I ran the SESTOS PID autotuning and let it go for 1-2 hours.
    b.  But I didn't check if autotuning completed before shutting off the power
2) Purged the ABS pellets until no ABS extrusion came out.
3) Raised the temperature to 220 C to prepare for the PETG pellets.
   a. Waited 10 minutes after reaching 220 C
   b. Then poured in PETG pellets.
   c. The extruded PETG diameter was 1.4 mm
   d. Lowered temperature to 190 C and lowered table height.
   e. Extruded filament diameter was now about 1.7 mm
   f.  But the filament coiled in a 4 inch circle - difficult to wind onto reel by hand!
   g. Shut down machine for the day.
4) Heated up Filastruder to 190 C and waited 10 - 20 minutes to stabilize temperature.
5)  Turned on motor
    a.  PETG filament started coming out.
    b.  Temperature dropped from 187 - 190 C to about 165 C in about 2 seconds.
    c.  Auger pipe turned 90 degrees clockwise (with auger rotation)
    d.  Auger stopped and gear box started knocking.

Notes:
I'm not sure if I correctly set the CC adjustment on the stall protection board.  I didn't hear the "soft click" the first time so I just turned it counter-clockwise enough that it should have been 0 and then turned it clockwise 7 turns.  After the catastrophe I realized that turning counter-clockwise past the "soft click" puts it back up to maximum current (I think).  I didn't know how to check if the CC adjustment was set correctly at the time.  If I understand correctly, now, hooking up the heater to the stall protection output terminals and turning the CC adjustment clockwise until you get 1.4-16 amps is a way to know positively that the stall protection is set for sure.  Somebody correct me if I am wrong here.

Also, I think the temperature drop to 165 C just before the catastrophe was because cooler PETG from the auger entered the chamber.  I think the PETG has a higher melt flow temperature than ABS and I may have needed to wait for a definite 30 minutes after thermocouple first reached 190 to ensure enough length of flowing PETG before turning on the motor.

7

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

I'm not sure if you prefer to troubleshoot via email or the forum - either is OK but lets keep it in one place or there other for clarity's sake and so no info gets lost.

A temperature drop of 25C in 2 seconds isn't physically possible, regardless of the temperature of the incoming PETG (which would have been preheated anyway). I suspect an issue with the thermocouple, perhaps it not being mounted securely and changing position when the motor started moving. So, that is something that needs to be checked into. I find that caption tape works well for securing it.

Yes, you can check the current limit with the heater. It is an extra unnecessary step and so I left it out of the instructions, but perhaps it is worth adding.

2.84 amps is definitely enough to damage the motor and the barrel. The current should not jump around like you're describing, I just tested with a heater and it held a rock steady reading. If after adjusting the CC pot you're not able to achieve a stead reading around 1.6A, then it would be good to exchange the stall protection board for a new one.

Let me know about the stall protection board and we'll go from there on any parts replacements.

8

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

I will use the forum to communicate then - I think this will benefit new users.   


Tim,  in a previous post (Help with Stall Protection Board - 2015-02-04 18:09:13) you wrote:

"
Oh, with a multimeter this is simple!
With the gearmotor unloaded and set to full voltage, you should see around 5.5RPM. One thing - because PWM is used to control motor voltage, it will always appear as ~12v to the multimeter.

Next, go full CCW on CV until you hear the click, disconnect the motor, connect the terminals for the multimeter. Set the meter to the 10A setting. Connect the meter terminals where the motor was. This will apply a short on the output of the motor. You can then adjust CV in the CW direction until you see 1.5 amps - this should be about 6 turns past the “0” point."


QUESTION:  Does this still apply?  So you use the CV to dial in the 1.5 amps?  Or was that meant to say CC?

9

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Typo, should have been CC. The V is for voltage, the C is for current. (The first C is for constant, or the limit)

If you link that post I'll go edit it to fix the typo.

10

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Here is the link:  http://www.soliforum.com/topic/9692/hel … ion-board/

Tim,

I now have a solid 1.5 amp (or whatever I want to dial in with CC adjustment) on the output of the stall protection board.  I confirmed it with both the heater hooked up to the stall protection board output terminals via graphical readout and also using the multimeter hooked up to the output terminals.   I think the fluctuations I was getting were because of two things: 1) I had the stall protection board resting on the aluminum chassis while I was testing it and/or 2) the wiring was messy so I fixed it up.   

I want to order the gears now and an auger tube+flange and a piece of Kapton tape so I can get this machine running again ASAP.  How do I order the auger tube+flange and tape if it doesn't show up on the order site?

11

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Oh, and now I believe my Filastruder died because I didn't have the CC set right because I didn't know how to test it so it was probably set to higher than 1.7 amps.  And my thermocouple was attached to the nozzle with a loop of silver solder which never melted but I think the Kapton tape will be better.

12

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

I just got my new gears and auger barrel.  Question:  does the metal spacer shown on the finger slide onto the shaft of gear 5 with the smaller diameter side touching gear 5?



http://soliforum.com/i/?QGZ1kqK.jpg

13

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

The purchase page for the gears shows the metal busing on top of gear 5 but the top of the case won't close with it there so it must be on the bottom of gear 5 with the smaller radius side of the bushing touching gear 5?

http://soliforum.com/i/?N2G8NcD.jpg

14

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Anyway,  I went ahead and put the bushing on the bottom of gear 5 and closed up the gearbox and reassembled the filastruder with the new auger barrel.   I have the CC set to 1.6 amps and CV set to 12 V and am extruding the Eastman PETG material. 

My Input Settings:
Temperature=220C
nozzle diameter = 1.75 but is probably actually 1.6 mm?
Table height = 2.5 feet
Exit fan is fully extended and extruded filament drapes over the PTFE tube

My Output:
Temperature reads 198 C
Current reads 1.6 amp all the time.
Extruded filament diameter = a very consistent 1.6 mm
Extrusion rate = 4 inch / minutes (shaft barely turning) then jumps to 24-30 inches / minute for 10 - 20 seconds then back to 6 inch / minute.

Questions:
1) Why won't the temperature rise above 198 C?
2) Is it ok for shaft to turn so slow while motor constantly at 1.6 amp?
3) Can I increase the amps?
4) Should I increase the nozzle diameter (drill it out)
5) Can anyone see anything wrong with my setup from the picture below?


http://soliforum.com/i/?mNSg5BU.jpg

15

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

1.) Not sure, perhaps excessive airflow across the nozzle. You could try scooting the insulation forward to shroud the nozzle better. What is the voltage across terminals 7 and 10 of the PID controller with the heater on?
2.) It is OK, but will increase wear on the gearbox. Not dramatically as that torque is within design parameters, but it is a larger load than 'normal'.
3.) You can, at your own risk. It is generally better to change other things instead. (Like increasing temperature to reduce gearmotor load)
4.) Yes, that would be a good idea. Nozzles are intentionally supplied undersize as it is easy to make a small hole larger, but not a large hole smaller. Some polymers exhibit considerable die swell and require a hole on the smaller end. Stock nozzles are drilled to 1.6mm. The other reason to supply undersize is that 1.6mm feeds and prints fine (just adjust in the slicer) but 1.9mm would jam most hotends.
5.) I would scoot the fan back so the center of the fan is under the face of the nozzle, and I'd raise everything to about 4 feet off the ground. Thermocouple held in place with silver solder is not advisable for two reasons - you're operating near solder's melting point, and caption would better field/insulate the thermocouple and allow it to get an accurate measurement.

I'd also recommend reading this writeup if you haven't already:

http://www.soliforum.com/topic/15657/co … -colorant/

16

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

I moved the insulation to shroud the nozzle, moved the the center of the fan under the nozzle exit, raised the filistruder nozzle exit height to 4 feet as you suggested above.  Additionally I drilled out the nozzle hole to 2 mm angled the filastruder with nozzle downward by about 30 degrees and set the temperature to 220 C.  So now it extrudes pretty good and the temperature stays near 220 C even though the stall board reads 1.6 amp pretty much all the time.  The Eastman PET filament diameter is 1.4 to 1.5 mm which is too thin.  I am going to follow the Eastman PET filament material review link and increase the nozzle diameter and temperature. 

NOW THE SCARY - so I noticed that the current jumped to 2.6 amp.  It was extruding fine but I shut it off quick.  I turned it on ant it was 2.3 amp but then the stall kicked in and current went down back down to 1.6 amp.  Is this normal?  Does the current sometimes go above the CC set current if nothing is stalling the motor?  Does the CV adjustment somehow allow the current to overshoot?

17

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

HELP HELP HELP

I turned on the filastruder and the stall protection board went up to 2.6 amp and the auger barrel spun 15 degrees!  I have to check if the the barrel is permanently damaged but I don't think it is because I was prepared and immediately turned off the motor.   Thankfully the auger barrel (pipe) wasn't completely tightened and thankfully I had extruded everything out of the pipe the night before.    Then unhooked the motor from the stall projection board and probed the output terminals with the ampmeter.  When I turned on the motor switch the current immediately read 2.6 amp but for only 1/2 second and went back to 1.6 amp.

18

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Turning 15deg isn't a big deal, it just means the barrel wasn't tightened enough when you installed the new one.

The value of the stall protection board limit shouldn't jump around. It sounds like something might be up with your stall protection board. It might have been damaged from back when it was set on a metal surface while powered. It might be good to pick up a new one, order from the store and reply to the order notification with a link to this thread and I'll refund the cost of the board as a courtesy.

When it hit 2.6 amps was the barrel fully heated? I would expect an empty, fully heated barrel to be a half amp or so of motor load.

19

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Ok,  I will order another stall protection board (I have the one with the graphical display).    I believe the 15 degree turn was a bad thing because the pipe had already turned 90 degrees due to hitting the 1.6 amp.   The finite element analysis I did on the pipe with the large opening indicated that 12 Newton-meter torque (correlating with 1.6 amp and 12 Volt according to the pdf assembly notes) was on the verge of yielding the steel barrel.  So 2.6 amp would definitely permanently deform the pipe except that thankfully the pipe wasn't fully tightened so it survived this recent episode.  I believe it is not a good idea to go over 1.6 or 1.7 amp to avoid yielding the steel pipe. 

The barrel was heated when the stall board read 2.6 amp and I thought it was uniformly hot enough but there must have been enough unmelted PETG in the chamber area to hold the end of the auger.  But the stall board should always keep the amps 1.6 and below right?  That way,  the barrel would be protected even if you turn on the motor with a cold system?

20

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

eric.s.hall.em wrote:

But the stall board should always keep the amps 1.6 and below right?  That way,  the barrel would be protected even if you turn on the motor with a cold system?

Yes.

Also, a couple other things. I suspect the FEA analysis you performed isn't quite right as I've experimentally loaded barrels higher without yielding (though I don't suggest this). It is rather challenging to get an FEA analysis to match real life, especially without knowing the alloy of steel being used. An FEA analysis is only as good as its input data.

It doesn't matter if the barrel is able to move or not, 2.5 amps worth of torque is 2.5 amps of torque. The barrel being able to rotate doesn't impact the stress experienced by the material, as the torque needed to accelerate the barrel is negligible.

Another possibility is incorrect assembly of the gearmotor, resulting in less than nominal torque for a given current. Though that wouldn't cause the current to jump around, it would explain why the 220C extrusion was causing the motor to reach overload. I'll check on that bushing placement tomorrow.

21

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Also I just saw that you applied a dead short to the output of the stall protection board. I would not advise that. Use a dummy load instead, like the heater. Current limiting circuits have a hard time with dead shorts.

22

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

I agree that physical experiment is better than FEA but at least FEA can give some insight.  And I also agree with you that I don't have the steel properties of the steel pipe (especially the yield stress which several sources indicate can be much higher - like 400 MPa instead of the 170 MPa I assumed).  But, for what it is worth, here are the initial FEA results based on these inputs:

Young's Modulus = 200 GPa
Poisson's ratio = 0.29
Yield Stress = 170 MPa
Tangent Modulus = 20 GPa (which is 10% of YM)
Torque = 12 Newton-Meter

The maximum stress with a 12 Newton-Meter torque at the end of the auger barrel is 174 MPa at the location in the image.  But this is just a localized stress and the average stress in the cutout region is more like 70 MPa which is well under the assumed 170 MPa yield stress. 





http://soliforum.com/i/?DQgV7Xo.jpg

23

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

It doesn't matter if the barrel is able to move or not, 2.5 amps worth of torque is 2.5 amps of torque. The barrel being able to rotate doesn't impact the stress experienced by the material, as the torque needed to accelerate the barrel is negligible.

Yes but it gives you time to shut the motor off before the pipe can't tighten anymore and the full torque is felt by the pipe.

24

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

The full torque is 'felt' by the pipe regardless of whether it is rotating or not. For a given shaft, torque at one end of the shaft is equal to torque at the other end of the shaft, assuming the shaft's angular acceleration term is negligible (which it is in this case).

Torque_in = Torque_out + alpha * I

Where Torque_in is the torque on one end of the shaft, Torque out is the torque at the other end, alpha is angular acceleration, and I is the moment of inertia. So in this case  if there's 10N-m applied at one end, the entire barrel is subjected to 10N-m whether it is rotating or not.

it is possible though that the motor hadn't reached its limit while the barrel was rotating. That would cause a lower torque than the limit to be applied to the barrel.

As for the gearmotor assembly, here's a fresh gearmotor:

http://imgur.com/a/2hP6c

25 (edited by eric.s.hall.em 2017-04-18 16:16:58)

Re: New User - Twisted the Auger Pipe and Stripped a Gear (Resolved)

Thanks for the gearbox assembly picture!

Yes, I agree that the torque at both ends of the barrel are equal (no angular acceleration) even though the barrel is turning.

But....
(Not including the motor efficiency in the input power calculation)
torque = power / angular velocity
power is 12 V x 1.5 amp = 18 Watts
angular velocity is about 14 rpm = 1.47 rad/sec

so torque = 18 Watts / 1.47 rad/sec =  12.24 Newton-meters.
With a 3 amp current (same angular velocity) the torque is 24.24 Newton-meters.
If the auger gets stuck and the angular velocity goes down to 0.5 rad/sec then wouldn't the torque go up to 72 Newton-meter

since torque = (12V x 3 amp) / 0.5 rad/sec = 72 Newton-meter?

I know I must be oversimplifying because if angular velocity goes to zero then the torque would be infinity which isn't true.

But if the auger barrel was able to turn still then the angular velocity of the barrel relative to the flange wouldn't decrease so suddenly - at least until the barrel pipe tightened to the flange.