Topic: Any ideas how to have more consistent diameter in this setup
Hi All
So here is my setup.
The barrel is about as insulated as its going to get with a cover plate with hold to shield the nozzle.
Nozzle is drilled to about 2.1
Filawinder and tube is mounted as secure as possible.
Pre-dried MG94 abs pellets with some colorant.
Motor and heater on different power supplies.
The filament coming out looks good, and the setup is running as reliably as i have ever been able to get.
In general, the diameter is right around 1.75 and generally stays there, but every so often it can drift up to 1.85 and down to 1.65. It seems to only do this for about 6" to a foot of length worth. If I measure the absolute worst spots its 1.61 - 1.9
The filament is generally still but i still see some sway when the filawinder turns off and on. Really can't think of a good way to stop that.
I'm running at about 194C. Speed is good, so I am thinking I will just drop temp and sacrifice speed and see what happens.
There are two fans behind the red thing, I have their voltage down to 3.3V so their is just a bit of cooling, but not enough to make the filament sway.
I kinda think its better for the first half hour or so when the filawinder tends to run consistently. Once the diameter of the spool gets bigger, it tends to start and stop. Is the firmware available for the filawinder? Maybe something can be tweaked there.
Also, the spool is really nice and tight now with the gauge adding tension, but occasionally the filament slips on itself on the spool, because the spooling isn't perfect. I'm sure that doesn't help, but I have no idea how make it spool better.
Also debating turning the fan off, and shortening the droop/temp as much as needed to get back up to 1.75... Anyone have success with no cooling on ABS?
Also, its a bit hard to really know my average diameter, as the filament really isn't circular. In the extreme I can see .05 -.1 of diameter change if i just rotate the filament.
I don't really think their is anything i can gain with automatic temp control, since the length that goes bad is only a foot or so, and the thickness gauge is about 5' away from the nozzle. So i'm left thinking the only real way to get better is to go with a direct pull setup, with a very short distance from nozzle to pull wheels, and then have active control. But i have no interest in doing that much work. In general the filament is usable and i think it kinda averages out when printing, but I would like to get a bit better.
Thanks for any thoughts.



