Topic: Fixing banding (z-wobble) with fine threaded z-rod
I was thinking... since the frequency of banding on the Solidoodle matches the thread spacing of the z-rod (18 threads per inch), why not just use a z-rod with a finer thread? Unlike other hardware solutions, which try to only minimize the "amplitude" of banding, using a finer thread would also change the frequency, instantly making it much less visible. The finer thread would also eliminate almost all backlash.
I decided to incorporate a couple of other improvements at the same time, so I used a very thin stainless steel M3 z-rod to benefit from its flexibility ($3.01 + $6.31 shipping):
http://www.ebay.com/itm/300885751211
This rod had a thread spacing of 0.5 mm, almost 3 times finer than the default z-axis rod.
And attach it using a small 5mm-3mm flexible helical coupling ($4.20 + $1.50 shipping)
http://www.ebay.com/itm/220977869760
For the new z-nut, I used a long brass spacer (pack of 10 - $4 + $2 shipping)
http://www.ebay.com/itm/250955139328
I found that M3 components are much more affordable than the larger components typically in demand for 3D printing applications.
I re-tapped the inside of the spacer to make sure the thread ran all the way through. If I had thought it out more fully before disassembling the z-carriage, I would have printed out some sort of holder adapter for the z-nut. Since I didn't, I just tapped most of the outside of the brass spacer and threaded on a larger nut and sealed it with locktite. With a short section of tubing, this nut fit snugly in the existing nut hugger.
Here is the assembled nut
And the printer with the installed z-rod
After reassembling, all I had to do was add some grease and increase the Z steps/mm value to 6400 (M92 Z6400). I did find I needed to turn down the maximum z speed from 5mm/s to 3mm/s (M203 Z3) to keep it moving reliably, but since the bed doesn't move much during printing, that seemed fine.
And here are the results from printing with no software compensation enabled. The object is a small octagonal cylinder printed at .1mm and viewed through a magnifying glass. The banding that was present before is now so slight and fine that it's negligible.