Topic: Tried for faster ABS extrusion, got tons of problems!
So, Tim recommended I bump the temp up from 194 to 204, bore out the nozzle to 1.8mm, and insulate the whole barrel. I did that and now I'm having nothing but trouble! Before, the filament would exit the nozzle, make a NICE loop, and get wound by the Filawinder. Now, it gets a ton of kinks and flails around all over the place.
It won't wind properly, because it gets stopped up on the sensor and then the filament just extrudes while the winder sits idle. If I sit there and manually guide the filament, I get it to work fine, but I'm absolutely not sitting there for 8 hours.
I tried everything I could think of, including using some PTFE tubing to act as a sort of guide, but nothing works! Eventually the filament always kinks up and starts to wind around and I have to stop the machine, cut off the filament, and start over with a spool of barely any filament! It's super wasteful.
I have my setup as shown here, but the box is flat rather than on it's side. I can't go back to 194 though, because I tried and it extrudes at or over 1.8mm and I'd rather not get jams as I print. What to do?
